Show I I t DRilliNG IS' IS RESUMED I II I IN 1 fAR INGTON fiElDS It was wa announced yesterday ny by the general manager of the Union Oil and I Jai all as company that the pece piece of pipe that had brol broken en off oft In well wen Xo No I 1 1 nr near nr-ar ar Farmington Farmington Farm- Farm ington inston and which has haR caused the com- com I so much trouble had been r recovered cov- cov ered cred the broken length taken out and ami a anew anew anew new one put In Its place and that active work worl In n sinking the tho thenell well nell to a greater I depth was resumed Q e eA A hea heavy flow Clow of or gas sas at this point should b hp ho encountered It Is stated around tho the foot GO level judging from the logs loss of or orthe the wells that w were ero driven In th the neighborhood neighborhood neigh neigh- twenty eight years ago This well I Is now down feet Tho The drillers I 1 encountered a heavy flow now of or ga gas ras at I foot The pressure was so gO stron strong that volumes of j sand land and water were thrown I ICO fret feet In the air The Tho pipe was driven on through this layer laer of or sand saml which was about abort seven feet thick This flow was II irr Insufficient u t for the company's compans use bu but butIs butIs t Is declared to be bl a stron strong Indication of or I what wh will be encountered at nt greater depths depth Considerable oil show was Valo In evidence Just before the pipe was broken last December Well cn No 2 Is down feet In this well quantities of or gas have been encountered encountered at various levels during the entire drilling |